Weight-Saving Features

In order to be successful in aviation use, the modern lightweight diesel of the time had to have its weight reduced from 25 lb/hp to 2.5 lb/hp. This required unusual design and construction methods, as follows:

Crankcase: It weighed only 34 lb because of three factors: Magnesium alloy was used extensively in its construction, thus saving weight as compared with aluminum alloy, which was the conventional material at this time. It was a single casting. This saved weight because heavy flanges, nuts, and bolts were dispensed with. The cylinders, instead of being bolted to the crankcase, as was normal practice, were held in position by two circular hoops of alloy steel passing over the cylinder flanges. They were tightened to such an extent that at no time did the cylinders transfer any tension loads to the crankcase. This type of fastening actually strengthened the crankcase in contrast to the usual method. For this reason it could be built lighter. The hoops did not always function well. “The first job I ever did on the Towle was to patch the holes in the top and bottom of the hull when a cylinder blew off during run-up and nearly beheaded the pilot.”[13]

Figure 22.—Rear view of engine with rear crankcase cover removed, showing valve and injector rocker levers and injector control ring mounted on crankcase diaphram. U.S. Navy test, 1931. (Smithsonian photo A48323D.)

Figure 23.—Main crankcase. U.S. Navy test, 1931. (Smithsonian photo A48325B.)

Figure 24.—Rear crankcase cover and gear train: crankshaft gear drives B, which drives oil pump at F. A, integral with B, drives internal cam gear. B also drives C on fuel-circulating pump. D, driven by crankshaft gear, drives E on generator shaft. U.S. Navy test, 1931. (Smithsonian photo A48325C.)

Figure 25.—Master and link connecting rods. U.S. Navy test, 1931. (Smithsonian photo A48323A.) Figure 26.—Crankshaft with automatic-timing retarding device on rear end of pivoted- and spring-mounted counterweights. U.S. Navy test, 1931. (Smithsonian photo A48323B.)
Figure 27.—Propeller hub and vibration damper. U.S. Navy test, 1931. (Smithsonian photo A48325A.)

Crankshaft: Since this engine developed the high maximum cylinder pressure of 1500 psi, it was necessary to protect the crankshaft from the resulting heavy stresses. Without such protection the crankshaft would be too large and heavy for practical aeronautical applications. Although the maximum cylinder pressures were 10 times as great as the average ones, they were of short duration. The method of protecting the crankshaft took full advantage of this fact. It consisted of having the counterweights flexibly mounted instead of being rigidly bolted, as was common practice. The counterweights were pivoted on the crank cheeks. Powerful compression springs absorbed the maximum impulses by permitting the counterweights to lag slightly, yet forced them to travel precisely with the crank cheeks at all other times.

Propeller Hub: The propeller is, of course, subject to the same stresses as the crankshaft. Instead of being rigidly bolted to the shaft as was common practice, it was further protected from excessive acceleration forces by being mounted in a rubber-cushioned hub. This permitted the use of a lighter propeller and hub.

Valves: A further weight saving resulted from the use of a single valve for each cylinder instead of two as in the case of conventional gasoline aircraft engines. (A diesel engine designed in this manner loses less efficiency than a gasoline one because only air is drawn in during the intake stroke.) In addition to the weight saving brought about by having fewer parts in the valve mechanism, there was an additional advantage since the cylinder heads could be made considerably lighter.

Figure 28.—Cylinder disassembly, showing valve and fuel injector.
U.S. Navy test, 1931. (Smithsonian photo A48324D.)