The meeting was in the North Quadrant of the Hokkaido facility, in the senior staff briefing room. The project kurirovat, Ivan Semenovich Lemontov, was at the head of the table as co-moderator. Flanked on his left was Petr Ivanovich Gladkov, the youthful director of aeronautics; Felix Vasilevich Budnikov, robust director of flight control systems; and Andrei Petrovich Androv, director of propulsion systems. On Lemontov's right was the other comoderator, the Japanese project director, Taro Ikeda.

Seated across the metal table, facing them all, was Yuri Andreevich Androv.

"We will begin today's agenda by reviewing Monday morning's test flight," Ikeda began, speaking in Russian. He was chairing the meeting as though by mutual consent. Soviet booster technology and aerodynamic know-how might be what made the project go, but when all was said and done, it was the money that talked. And the project financing was Japanese. "The pilot's report will be our first item."

Yuri nodded and glanced at the notes on the table before him. Make this quick, he told himself.

"I'm happy to report that, once again, the handling characteristics of the vehicle correlated closely with our up-and-away simulation in the Fujitsu SX-10. On takeoff the vehicle rotated very nicely into a lift-off attitude of six point five degrees. My target attitude was seven point five degrees, and once I'd captured that I accelerated out to seven hundred knots, then climbed to forty-nine thousand feet for the first series of maneuver blocks—the roll maneuvers, pitch maneuvers, and yaw maneuvers—intended to verify handling characteristics and control activity at high altitude. As on all other flights, the directional stability was excellent, with a very large restoring moment. In the yaw maneuvers, one rudder kick gave me an overshoot but the vehicle immediately steadied. And the pitch maneuvers again showed that her actuating system enhances stability very fast. In fact, all maneuvers matched our simulations within acceptable limits. I also did some banks up to fifty degrees to get the stick force as I pulled back. The turn performance matched specifications, with very little control activity required. I also carried out some bank-to- bank maneuvers, to get the roll rates; the block included quarter stick, half stick, and three-quarter stick. Very stable. The augmented controls did not move out, that is, move around a lot."

He paused for breath, stealing a glance at the room. Just bury them in data overload, he thought. Don't give them time to ask questions.

Before anyone could speak, he pressed on. "I also took the vehicle through the prescribed block of throttle maneuvers. Remember that in ramjet mode the engines are fan-controlled, with all controls in the initial stage. As scheduled, I pulled all the throttles to idle and then took them all the way up to rated thrust. And as always, they were very responsive and didn't have to hunt for their setting."

"Good," Ikeda said, "but the main reason—"

"Exactly. As scheduled, at 0210 hours I terminated JP-7 feed to the portside outboard trident, causing an unstart. With asymmetric thrust, I expected adverse yaw, as in the roll maneuver, but the control system stabilized it immediately. I also assumed there'd be some sideslip, so I put rudder in, but then I realized handling was going to be feet on the floor. This vehicle is a dream." He paused to smile. "Anyway, I then initiated restart at 0219 hours." He shoved forward the documents piled by his side. "These charts indicate that rpm achieved ninety percent nominal within eleven seconds. All the—"