X Corps had received orders on 1 December for the 3d Infantry Division to assemble in the Wonsan area prepared for further operations, possibly to join the Eighth Army in west Korea. Although General Almond initiated execution of the order immediately, he sent the highest ranking Marine officer on his staff, Colonel Forney, and the Corps G-2, Lieutenant Colonel William W. Quinn, to Tokyo to explain the implications of the withdrawal of this Army division from northeast Korea. Following a conference with General Hickey, GHQ Chief of Staff, the Division was released back to X Corps on the 3d, and General Almond ordered it to return to the Hamhung area to protect this vital port area and to assist the breakout of the 1st Marine Division by relieving 1/1 at Chinhung-ni.[583]

[583] X Corps Special Report, Chosin Reservoir, 17–18; Forney, Special Report, 3.

At 2115 on 6 December the 1st Marine Division requested by dispatch that the relief be completed the next day in order to free 1/1 for the attack to the north. The relief column, designated Task Force Dog and commanded by Brigadier General Armistead D. Mead, ADC of the 3d Infantry Division, consisted of the 3d Battalion, 7th Infantry, the 92d Armored Field Artillery Battalion, plus detachments of engineers, signalmen, and antiaircraft troops. Brushing aside some Chinese roadblocks, it arrived at Chinhung-ni on the afternoon of the 7th and relieved 1/1 immediately.[584]

[584] Smith, Notes, 1063–1064; X Corps Special Report, Chosin Reservoir, 20–24; X Corps OI 26, 5 Dec 50; and Dolcater, 3d Infantry Division in Korea, 90; CG 1stMarDiv msg to CG X Corps, 2115 6 Dec 50; CG X Corps msg X 13811, 7 Dec 50; Col D. M. Schmuck Comments, n. d.

Air Drop of Bridge Sections

Another problem which the 1st Marine Division planners had faced at Hagaru called for an engineering solution. As early as 4 December the commanding general was notified that a critical bridge three and a half miles south of Koto-ri (see Map 29) had been blown by the enemy for the third time. At this point water from the Chosin Reservoir was discharged from a tunnel into four penstocks, or large steel pipes, which descended sharply down the mountainside to the turbines of the power plant in the valley below. Where the pipes crossed the road, they were covered on the uphill side by a concrete gatehouse, without a floor. On the downhill side was the one-way bridge over the penstocks which the enemy had thrice destroyed. Between the cliff and the sheer drop down the mountainside there was no possibility of a bypass. Thus the gap of 16 feet (24 feet, counting the abutments) must be spanned if the Division was to bring out its vehicles, tanks and guns.[585]

[585] Except when otherwise specified, this section is based on the following sources: Partridge interv, 25 Jun 51, 48–63; Litzenberg interv, 27–30 Apr and 15 Jul 51, 72–73; Smith, Notes, 1057–1059, 1075, 1095–1109; 1stEngBn SAR, 3–14; Geer, The New Breed, 361–362, 369; LtCol J. H. Partridge Comments, n. d.

Following the destruction of the original concrete bridge, the enemy had blown a temporary wooden structure and an M-2 steel treadway span installed by Army engineers. No prefabricated bridging was available at Hagaru, and time did not permit the construction of a timber trestle bridge. The possibility of Bailey bridge sections was considered but rejected for technical reasons. Finally, after a detailed study of the break from the air on 6 December, Lieutenant Colonel Partridge estimated that four sections of an M-2 steel treadway bridge would be required. Prospects did not appear bright when a bridge section was badly damaged on the 6th after being test-dropped at Yonpo by an Air Force C-119. Nevertheless, it was decided to go ahead the next day with the drop at Koto-ri.[586]

[586] Smith, Notes, 1057–1059, 1075, 1095–1097; Partridge interv, 25 Jun 51, 48–53; 1stEngBn SAR, 13–14.