With the exception of the English lime, all grout was mixed 1 to 1 with sand in a Cockburn continuous-stirring machine operated by a 3-cylinder air engine. The grout machine was placed on the lower floor of the trailing platform shown on [Plate LXXII], while the materials were placed on the upper platform, and, together with the water, were fed into the machine through a hole in the upper floor. The sand was bagged in the yard, and the cars on which the materials were sent into the tunnels were lifted by an elevator to the level of the upper floor of the trailing platform before unloading.

Great difficulty was experienced in preventing the waste of the fluid grout ahead of the shield and into the tail through the space between it and the iron lining. In a full soft ground section, the first condition did not usually arise. In the full-rock sections the most efficient method of checking the waste was found to be the construction of dams or bulkheads outside the lining between it and the rock surface. For this purpose, at intervals of about 30 ft., the leading ring and the upper half of the preceding one were disconnected and pulled forward sufficiently to give access to the exterior. A rough dam of rubble, or bags of mortar or clay, was then constructed outside the iron, and the rings were shoved back and connected up. In sections containing both rock and soft ground, grout dams were built at the cutting edge at intervals, and were carried up as high as circumstances permitted.

The annular space at the tail of the shield was at all times supposed to be packed tight with clay and empty bags, but the pugging was difficult to maintain against the pressure of the grout. For a time, 1/2-in. segmental steel plates, slipped down between the jackets and the iron, were used to retain the pugging, but their displacement resulted in a number of broken flanges, and their use was abandoned. In their place, 2-in. segmental plates attached to the jack heads were substituted with more satisfactory results. Notwithstanding these devices, the waste of grout at the tail was very great.

The soft ground material on various portions of the work acted very differently. The clay and "bull's liver" did not cave in upon the iron lining for several hours after the shield had passed, sometimes not for a day or more, which permitted the space between it and the iron to be grouted. The fine gray or beach sand and the quicksand closed in almost at once. The quicksand has a tendency to fill in under the iron from the sides and in places to leave a cavity at about the horizontal diameter which was not filled from above, as the sand, being dried out by the air, stood up fairly well and did not cave against the iron, except where nearly horizontal at the top.

The total quantity of grout used on the work was equivalent in set volume to 249,647 bbl. of 1 to 1 Portland cement grout, of which 233,647 bbl. were ejected through the iron lining, an average of 14.93 bbl. per lin. ft. The cost of grout ejected outside of the river tunnels was 93 cents per bbl. for labor and $2.77 for "top charges." East of the Long Island shaft the corresponding costs were $0.68 and $1.63, the difference being partly due to the large percentages of work done in the normal air at the latter place.

Caulking and Leakage.

Up to August, 1907, the joints between the segments of the cast-iron lining were caulked with iron filings and sal ammoniac, mixed in the proportion of 400 to 1 by weight. With the air pressure balancing the hydrostatic head near the tunnel axis, it was difficult to make the rust-joint caulking tight below the axis against the opposing water pressure; this form of caulking was also injured in many places by water dripping from service pipes attached to the tunnel lining. A few trials of lead wire caulked cold gave such satisfactory results that it was adopted as a substitute. Pneumatic hammers were used successfully on the lead caulking, but were only used to a small extent on the rust borings, which were mostly hand caulked. Immediately before placing the concrete lining, all leaks, whether in the rust borings or lead, were repaired with lead, and the remainder of the groove was filled with 1 to 1 Portland cement mortar, leaving the joints absolutely water-tight at that time. The subsequent development of small seepages through the concrete would seem to indicate that the repair work should have been carried on far enough in advance of the concreting to permit the detection of secondary leaks which might develop slowly. The average labor cost chargeable against the caulking was 12 cents per lin. ft., to which should be added 21.8 cents for "top charges."

Unfortunately, it was necessary to place the greater part of the concrete lining in the river tunnels during the summer months when the temperature at the point of work frequently exceeded 85°; and the temperature of the concrete while setting was much higher. This abnormal heat, due to chemical action in the cement, soon passed away, and, with the approach of winter, the contraction of the concrete resulted in transverse cracks. By the middle of the winter these had developed quite uniformly at the ends of each 30-ft. section of concrete arch as placed, and frequently finer cracks showed at about the center of each 30-ft. section.

While the temperature of the concrete was falling, a like change was taking place in the cast-iron lining, with resulting contraction. The lining had been erected in compressed air, the temperature of which averaged about 70° in winter and higher in summer. Compressed air having been taken off in the summer of 1908, the tunnels then acquired the lower temperature of the surrounding earth, slowly falling until mid-winter. The contraction of the concrete, firmly bedded around the flanges of the iron, and showing cracks at fairly uniform intervals, probably localized the small corresponding movements of the iron near the concrete cracks, and resulted in a loosening of the caulking at these points. With the advent of cold weather, damp spots appeared in numerous places on the concrete, and small seepages showed through quite regularly at the temperature cracks, in some cases developing sufficiently to be called leaks. Only a few, however, were measurable in amount.

Early in January small brass plugs were firmly set on opposite sides of a large number of cracks, and caliper readings and air temperature observations were taken regularly throughout the winter and spring. The widths of the cracks and the amount of leakage at them increased with each drop in temperature and decreased as the temperature rose again, but until spring the width of the cracks did not return to the same point with each return of temperature.